Replacing the E39 Valve Cover Gasket and VANOS Seals

Leaky valve cover gaskets (aka VCG) are probably one of the most common problems with older BMWs. The E39 is no exception. When the problem gets bad enough, oil will leak into the exhaust manifold, where it will smoke and is a fire hazard. So, when I noticed oil smoke in the engine bay of my E39, I decided the VCG was past due for replacement. And what better opportunity to do the VANOS seals while everything is opened up? So, that is exactly what I did.

VANOS is to BMW as V-TEC is to Honda. Essentially, the VANOS unit adjusts the engine timing to improve drivability and performance. The VANOS unit has two pistons, one for each of the camshafts. These pistons have seals, and these seals are what go bad. Quickly. From the BMW factory in Germany, buna-n rubber seals were used. This material the opposite of ideal for this application, and this leads to their early failure. As a result, this job is considered by many BMW enthusiasts as a good way to regain lost performance.

This is the engine after I removed the cover but before I removed the coils.

I began the job on a Friday night by removing the engine cover, coils, and valve cover. This was all very simply, although I had previously had trouble removing a stuck cap nut that held the valve cover down. Once the valve cover gasket was removed, it was time to remove the VANOS unit.

This is the front of the engine with the valve cover and VANOS unit removed. The timing chain is showing.

I was also surprised at the simplicity of the work. Compared to suspension work, or even brake work, the VANOS unit removal was very simply. It required the use of an 8mm hex socket, as well as needle nose pliers, a torx bit, and some sockets. Previously, I had also disconnected four electrical connectors for the VANOS solenoids, etc. Once removed, I took out both of the VANOS pistons to gain access to the worn seals. This is where my work ended for the night.

The next morning, I got up early to continue where I’d left off. I began by cutting out the old VANOS seals using an X-Acto knife. In order to get the new seals in the grooves (two seals in each of the four grooves), I had to soak them in warm water, as the teflon (the new material of the seals) was cold and stiff. Once warmed, I was able to stretch the new seals into place. It was now time for reassembly.

These as the VANOS pistons. They slide back and forth inside the VANOS unit to adjust timing parameters.

First, I put the pistons back into the VANOS unit. This involved removing and replacing them a few times to get the new seals to resize to the correct size. Once this was completed, I put in a new gasket between the VANOS unit and the head. I had cleaned the VANOS unit and the head mating surfaces with brake cleaner previously, so everything was ready to go back together. I slid the VANOS unit back onto the head studs and torqued it down. I then plugged in all of the electrical connectors. It was time to put the valve cover back on. I put new gaskets on the valve cover and put some gasket sealer on the head surface in the corners where the gasket might have trouble sticking. I then aligned the cover and placed it on the head, taking care to not trap any wires at the back of the engine. I then replaced the cap nuts and rubber grommets that hold down the valve cover. I torqued these down, replaced the coil packs, replaced the engine cover, and was ready to rumble. It was time to start the car.

In this image, I am torquing down the covers on the VANOS unit using the 8mm hex socket.

Immediately the car fired to life. Pulling out of the garage, I already noticed an improvement in low-end power, as fewer revs were needed to move. I took the car around the block, and working the clutch became much easier. I couldn’t believe the difference replacing the seals had made.

Completing a project like this feels really good. It is so satisfying to fix something or make something better that I felt like jumping right into the next project. I even stated to my mom that I fee comfortable doing even more complex repairs, and said that, if I had to, I would drop the transmission and replace the clutch myself. A few days later, the ‘high’ has worn off and I’m not actually so sure that I could have as much success with removing the transmission as I did with this last job, but who knows. Luckily, my clutch doesn’t seem to be requiring replacement.

He wasn’t very helpful.

 

Oil Change

I’ve changed the oil in my car once before, but never by myself. However, being such an easy job, I figured I’d do it in my grandparents’ driveway. At their house, I learned that my front bumper was too low to drive onto my grandfather’s ramps, so I figured I’d jack the car up and set it down on the ramps. However, I couldn’t even fit the jack underneath the car to get at the center jacking point, so I had to lift each side individually on two-by-fours, until I could fit the jack under the center point. I then lifted the car up and put it on the ramps.

The rest of the job was a breeze. I took out the old oil filter and removed it from the housing. I put a new rubber gasket and filter in the cap of the housing. I removed the drain plug and let the oil drain out. Then, I put the new oil in the car after putting the new filter in. Some guy rolled his window down and asked me when he should be dropping his truck off for an oil change. I torqued everything down after putting in 6.5 liters, and put the car back on the ground (the reverse of the lifting process). All in all, it was a successful job.

Valve Cover Bolt

It has been months since I first tried to change the valve cover gasket and VANOS seals in my E39 BMW. I was stopped in my tracks due to a stuck valve cover bolt, which proceeded to strip. I tried cutting a slot and inserting a screw driver, drilling a hole to get penetrating solvent in there, but nothing worked. I was getting very frustrated, and the valve cover was leaking badly enough that the car would smoke every once in a while from oil burning on the exhaust manifold. It was time do something about this.

I brought the car to my independent mechanic, who was able to get the bolt off by using a chisel at the right angle and tapping it. This finally caused the seize to break and the bolt became free. Now, I can finally, months later, make my second attempt at changing my valve cover gasket and VANOS seals.

E39 Front Brake Job

This past weekend, I had four days off school, which allowed me to complete my long-needed front brake job. I had been experiencing occasional “check brake linings” messages, as well as squealing when stopping. Finally, I had the time to do the job.

While I was at the Bavarian Autosport Show and Shine this past September, I talked with a fellow E39 owner about changing the pads and rotors. He gave me a few tips that would be helpful should the rotors be seized onto the hubs. Luckily for me, they were not.

I began the job around 5pm on a Friday, using my mother’s garage bay, as hers has much more space and better lighting than mine. While I was down at Bavarian Autosport in New Hampshire prior to the Show and Shine, I bought new Meyle brake rotors and Jurid Pads. Unfortunately, I overlooked buying a new wear sensor, which I had to order at a later date (and pay criminal shipping charges from New Hampshire to Midcoast Maine).

The job started off well; my new jack worked smoothly and I was able to get my car securely lifted on a jack stand. I then proceeded to remove the passenger side wheel to access the brakes. I removed the caliper, which was held into the caliper bracket by two (7mm?) Allen key bolts. I placed the caliper on a fishing tackle box, which was the perfect height to prevent the caliper from hanging from the brake lines. It is often suggested to simply zip-tie the caliper to the coils of the springs to avoid hanging it from the lines, but the fishing-tackle-box idea seemed more secure. Next, I removed the caliper bracket by removing the two bolts with a six-point socket. Now, it was time to remove the rotor.

I had heard that the little Allen bolt that holds on the rotors can strip easily. Worse, I had heard that they are often seized. Knowing my car, I highly suspected this was the case. To my happiness, the bolt came right out with a little tap with a rubber mallet on the end of the racket. I was able to take off the rotor. Now, it was time to put things back together, which is always twice as difficult as taking them apart.

Luckily, the only problem I ran into during the reassembly process was getting the calipers back on the rotors, as I didn’t have a “piston pusher” to push the brake pads back. I was able to overcome this and complete the job successfully.